So the engine is all back together now.
I haven't as been good at posting the last few weeks, lots of stress at work.
Here is a recap of the last few weeks.
I got all the parts I ordered and started putting the engine back together. This took about 6 hours over 2 days. Unfortunately I damaged the clutch side seal trying to use a crank puller that was designed for other models. So I had to wait till the next weekend after a bought a new seal to complete the assembly.
The following weekend I put the seal in and got the clutch in, but the clutch did not fit right. I put the number of clutch plates as in the parts layout. But the kit I got was different, so after figuring out the clutch was not fitting properly, I took it back out and added the extra plate and cork and the unit fit properly back in.
I put on the new piston, cylinder and head, then put on the new stator and flywheel. Getting the wires through the case was problematic, but eventually I got them through.
Then I started to put the engine back in the frame. The person who was going to help was sick so I had to put in by my self. After a few attempts and bloody scratches, accidently pushed the frame over. I decided to leave it on its side and was able to put the engine in much easier.
Once the engine was in, I stopped for the weekend.
The next weekend I worked on the wiring, since with the new stator, the wiring was a little different. I got the wiring to a point where I thought I could start the scooter. I put the gas tank back on and took the scooter outside and put some gas in it. I opened the fuel valve and pulled out the choke. There was a gas leak around the carburetor, it turned out to be a missing gasket on one of the screws.
After the leak was taken care of, the gas back on, I kicked it over. Then again and it started up. Second kick start, I was overjoyed. Happy dance!
After a little celebration, I got out the timing light to check the timing. It showed the timing was at about 12 TDC not the recommended 22. So back to the workshop, remove the flywheel and I adjusted the stator as far as it would go, but it did not make 22 BTDC. I put the flywheel back on and started the scooter, this time it was at about 17 BTDC. So back to the shop, I removed the flywheel then I removed the stator and drilled holes where 22 BTDC should be. I put the stator back on, again having to feed the wires that barely fit through the engine case and hooked up the wiring. Since it was raining I decided to work on the brake switch. The switch needed to be swapped out with a new one for the new stator arrangement and this proved to be a bigger project than I thought it would be. I ended up also replacing the brake cable and housing. This took about 2 hours.
After that there was a lull in the rain, so I took the scooter back outside and started it up. But with the muddy ground and the chance of rain starting back up, I decided to wait until the next weekend to check the timing on the new stator setup.
So put the scooter back inside and cleaned up the shop before heading home.